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< Natural Gas and Oil > Editorial Department
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Issue:ISSN 1006-5539
          CN 51-1183/TE

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    Your Position :Home->Past Journals Catalog->2014 Vol.4

    Technology for Natural Gas Loss Control
    Author of the article:Gong Maodi, Li Junqiang, Li Yangyang, Liang Guangqiang, Li Yanqin, Bi Xiumei
    Author's Workplace:SINOPEC Zhongyuan Oilfield Company Puguang Branch Natural Gas Purification Plant
    Key Words:Consumption control; Flash steam; High sour gas; Influence factor
    Abstract:

    Puguang gas purification plant, with an annual gas processing capacity of 120 x 108m3 and an annual purified gas output capacity of 93 x 108m3 is the first high sour gas purification plant with 100 x 108m3 processing capacity in China up to now. Natural gas consumption amount is very large due to its large processing capacity. In order to control and reduce gas consumption as far as possible, optimized are technological process and design parameters and analyzed are causes of large gas consumption. Taken are such measures as decreasing gas consumption during startup and shutdown, increasing flash steam recovery and utilization and lowering self-used gas of equipment, accordingly, gas consumption amount of the plant is greatly reduced. The study result can provide valuable reference for other high sour gas processing units.


     


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