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Issue:ISSN 1006-5539
          CN 51-1183/TE

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    Your Position :Home->Past Journals Catalog->2016 Vol.6

    Study on Increasing Operating Rate for Tail Gas Treatment Unit in Longgang Gas Processing Plant
    Author of the article:Yan Chongrong, Lei Yu, Huang Jun
    Author's Workplace:1.PetroChina Southwest Oil & Gasfield Company. Chuanzhong Gas Field;2.China Petroleum Engineering Co., Ltd. Southwest Company
    Key Words:Natural gas processing; Tail gas treatment unit; Corrosion; Operating rate
    Abstract:For constant S02 effluent rate28.lkg/h and ensuring achieving environmental protection requirement, tail gas treatment unit is an important environmental protection facility and its operating rate must be increased. By analyzing operation condition and shutdown condition of tail gas treatment unit in Longgang gas processing plant and studying shutdown caused by solvent corrosion and other factors, updated operation methods were raised, as well as measures for solvent corrosion control, and the operating rate were increased, and solutions and suggestions for operation and maintenance were proposed.

     


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